- 04 8月, 2015 1 次提交
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由 Mathias Nyman 提交于
We need to check that a TRB is part of the current segment before calculating its DMA address. Previously a ring segment didn't use a full memory page, and every new ring segment got a new memory page, so the off by one error in checking the upper bound was never seen. Now that we use a full memory page, 256 TRBs (4096 bytes), the off by one didn't catch the case when a TRB was the first element of the next segment. This is triggered if the virtual memory pages for a ring segment are next to each in increasing order where the ring buffer wraps around and causes errors like: [ 106.398223] xhci_hcd 0000:00:14.0: ERROR Transfer event TRB DMA ptr not part of current TD ep_index 0 comp_code 1 [ 106.398230] xhci_hcd 0000:00:14.0: Looking for event-dma fffd3000 trb-start fffd4fd0 trb-end fffd5000 seg-start fffd4000 seg-end fffd4ff0 The trb-end address is one outside the end-seg address. Cc: <stable@vger.kernel.org> Tested-by: NArkadiusz Miśkiewicz <arekm@maven.pl> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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- 23 7月, 2015 1 次提交
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由 Zhuang Jin Can 提交于
When the link is just waken, it's in Resume state, and driver sets PLS to U0. This refers to Phase 1. Phase 2 refers to when the link has completed the transition from Resume state to U0. With the fix of xhci: report U3 when link is in resume state, it also exposes an issue that usb3 roothub and controller can suspend right after phase 1, and this causes a hard hang in controller. To fix the issue, we need to prevent usb3 bus suspend if any port is resuming in phase 1. [merge separate USB2 and USB3 port resume checking to one -Mathias] Cc: <stable@vger.kernel.org> Signed-off-by: NZhuang Jin Can <jin.can.zhuang@intel.com> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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- 31 5月, 2015 2 次提交
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由 Mathias Nyman 提交于
Fix the xhci driver from bluntly setting the transferred length to 0 if we get a STALL on anything else than the data stage of a control transfer. Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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由 Roger Quadros 提交于
The problem seems to be that if a new device is detected while we have already removed the shared HCD, then many of the xhci operations (e.g. xhci_alloc_dev(), xhci_setup_device()) hang as command never completes. I don't think XHCI can operate without the shared HCD as we've already called xhci_halt() in xhci_only_stop_hcd() when shared HCD goes away. We need to prevent new commands from being queued not only when HCD is dying but also when HCD is halted. The following lockup was detected while testing the otg state machine. [ 178.199951] xhci-hcd xhci-hcd.0.auto: xHCI Host Controller [ 178.205799] xhci-hcd xhci-hcd.0.auto: new USB bus registered, assigned bus number 1 [ 178.214458] xhci-hcd xhci-hcd.0.auto: hcc params 0x0220f04c hci version 0x100 quirks 0x00010010 [ 178.223619] xhci-hcd xhci-hcd.0.auto: irq 400, io mem 0x48890000 [ 178.230677] usb usb1: New USB device found, idVendor=1d6b, idProduct=0002 [ 178.237796] usb usb1: New USB device strings: Mfr=3, Product=2, SerialNumber=1 [ 178.245358] usb usb1: Product: xHCI Host Controller [ 178.250483] usb usb1: Manufacturer: Linux 4.0.0-rc1-00024-g6111320 xhci-hcd [ 178.257783] usb usb1: SerialNumber: xhci-hcd.0.auto [ 178.267014] hub 1-0:1.0: USB hub found [ 178.272108] hub 1-0:1.0: 1 port detected [ 178.278371] xhci-hcd xhci-hcd.0.auto: xHCI Host Controller [ 178.284171] xhci-hcd xhci-hcd.0.auto: new USB bus registered, assigned bus number 2 [ 178.294038] usb usb2: New USB device found, idVendor=1d6b, idProduct=0003 [ 178.301183] usb usb2: New USB device strings: Mfr=3, Product=2, SerialNumber=1 [ 178.308776] usb usb2: Product: xHCI Host Controller [ 178.313902] usb usb2: Manufacturer: Linux 4.0.0-rc1-00024-g6111320 xhci-hcd [ 178.321222] usb usb2: SerialNumber: xhci-hcd.0.auto [ 178.329061] hub 2-0:1.0: USB hub found [ 178.333126] hub 2-0:1.0: 1 port detected [ 178.567585] dwc3 48890000.usb: usb_otg_start_host 0 [ 178.572707] xhci-hcd xhci-hcd.0.auto: remove, state 4 [ 178.578064] usb usb2: USB disconnect, device number 1 [ 178.586565] xhci-hcd xhci-hcd.0.auto: USB bus 2 deregistered [ 178.592585] xhci-hcd xhci-hcd.0.auto: remove, state 1 [ 178.597924] usb usb1: USB disconnect, device number 1 [ 178.603248] usb 1-1: new high-speed USB device number 2 using xhci-hcd [ 190.597337] INFO: task kworker/u4:0:6 blocked for more than 10 seconds. [ 190.604273] Not tainted 4.0.0-rc1-00024-g6111320 #1058 [ 190.610228] "echo 0 > /proc/sys/kernel/hung_task_timeout_secs" disables this message. [ 190.618443] kworker/u4:0 D c05c0ac0 0 6 2 0x00000000 [ 190.625120] Workqueue: usb_otg usb_otg_work [ 190.629533] [<c05c0ac0>] (__schedule) from [<c05c10ac>] (schedule+0x34/0x98) [ 190.636915] [<c05c10ac>] (schedule) from [<c05c1318>] (schedule_preempt_disabled+0xc/0x10) [ 190.645591] [<c05c1318>] (schedule_preempt_disabled) from [<c05c23d0>] (mutex_lock_nested+0x1ac/0x3fc) [ 190.655353] [<c05c23d0>] (mutex_lock_nested) from [<c046cf8c>] (usb_disconnect+0x3c/0x208) [ 190.664043] [<c046cf8c>] (usb_disconnect) from [<c0470cf0>] (_usb_remove_hcd+0x98/0x1d8) [ 190.672535] [<c0470cf0>] (_usb_remove_hcd) from [<c0485da8>] (usb_otg_start_host+0x50/0xf4) [ 190.681299] [<c0485da8>] (usb_otg_start_host) from [<c04849a4>] (otg_set_protocol+0x5c/0xd0) [ 190.690153] [<c04849a4>] (otg_set_protocol) from [<c0484b88>] (otg_set_state+0x170/0xbfc) [ 190.698735] [<c0484b88>] (otg_set_state) from [<c0485740>] (otg_statemachine+0x12c/0x470) [ 190.707326] [<c0485740>] (otg_statemachine) from [<c0053c84>] (process_one_work+0x1b4/0x4a0) [ 190.716162] [<c0053c84>] (process_one_work) from [<c00540f8>] (worker_thread+0x154/0x44c) [ 190.724742] [<c00540f8>] (worker_thread) from [<c0058f88>] (kthread+0xd4/0xf0) [ 190.732328] [<c0058f88>] (kthread) from [<c000e810>] (ret_from_fork+0x14/0x24) [ 190.739898] 5 locks held by kworker/u4:0/6: [ 190.744274] #0: ("%s""usb_otg"){.+.+.+}, at: [<c0053bf4>] process_one_work+0x124/0x4a0 [ 190.752799] #1: ((&otgd->work)){+.+.+.}, at: [<c0053bf4>] process_one_work+0x124/0x4a0 [ 190.761326] #2: (&otgd->fsm.lock){+.+.+.}, at: [<c048562c>] otg_statemachine+0x18/0x470 [ 190.769934] #3: (usb_bus_list_lock){+.+.+.}, at: [<c0470ce8>] _usb_remove_hcd+0x90/0x1d8 [ 190.778635] #4: (&dev->mutex){......}, at: [<c046cf8c>] usb_disconnect+0x3c/0x208 [ 190.786700] INFO: task kworker/1:0:14 blocked for more than 10 seconds. [ 190.793633] Not tainted 4.0.0-rc1-00024-g6111320 #1058 [ 190.799567] "echo 0 > /proc/sys/kernel/hung_task_timeout_secs" disables this message. [ 190.807783] kworker/1:0 D c05c0ac0 0 14 2 0x00000000 [ 190.814457] Workqueue: usb_hub_wq hub_event [ 190.818866] [<c05c0ac0>] (__schedule) from [<c05c10ac>] (schedule+0x34/0x98) [ 190.826252] [<c05c10ac>] (schedule) from [<c05c4e40>] (schedule_timeout+0x13c/0x1ec) [ 190.834377] [<c05c4e40>] (schedule_timeout) from [<c05c19f0>] (wait_for_common+0xbc/0x150) [ 190.843062] [<c05c19f0>] (wait_for_common) from [<bf068a3c>] (xhci_setup_device+0x164/0x5cc [xhci_hcd]) [ 190.852986] [<bf068a3c>] (xhci_setup_device [xhci_hcd]) from [<c046b7f4>] (hub_port_init+0x3f4/0xb10) [ 190.862667] [<c046b7f4>] (hub_port_init) from [<c046eb64>] (hub_event+0x704/0x1018) [ 190.870704] [<c046eb64>] (hub_event) from [<c0053c84>] (process_one_work+0x1b4/0x4a0) [ 190.878919] [<c0053c84>] (process_one_work) from [<c00540f8>] (worker_thread+0x154/0x44c) [ 190.887503] [<c00540f8>] (worker_thread) from [<c0058f88>] (kthread+0xd4/0xf0) [ 190.895076] [<c0058f88>] (kthread) from [<c000e810>] (ret_from_fork+0x14/0x24) [ 190.902650] 5 locks held by kworker/1:0/14: [ 190.907023] #0: ("usb_hub_wq"){.+.+.+}, at: [<c0053bf4>] process_one_work+0x124/0x4a0 [ 190.915454] #1: ((&hub->events)){+.+.+.}, at: [<c0053bf4>] process_one_work+0x124/0x4a0 [ 190.924070] #2: (&dev->mutex){......}, at: [<c046e490>] hub_event+0x30/0x1018 [ 190.931768] #3: (&port_dev->status_lock){+.+.+.}, at: [<c046eb50>] hub_event+0x6f0/0x1018 [ 190.940558] #4: (&bus->usb_address0_mutex){+.+.+.}, at: [<c046b458>] hub_port_init+0x58/0xb10 Signed-off-by: NRoger Quadros <rogerq@ti.com> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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- 10 5月, 2015 2 次提交
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由 Joe Lawrence 提交于
If the xHCI host controller has died (ie, device removed) or suffered other serious fatal error (STS_FATAL), then xhci_irq should handle this condition with IRQ_HANDLED instead of -ESHUTDOWN. Signed-off-by: NJoe Lawrence <joe.lawrence@stratus.com> Cc: <stable@vger.kernel.org> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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由 Mathias Nyman 提交于
Isoc TDs usually consist of one TRB, sometimes two. When all goes well we receive only one success event for a TD, and move the dequeue pointer to the next TD. This fails if the TD consists of two TRBs and we get a transfer error on the first TRB, we will then see two events for that TD. Fix this by making sure the event we get is for the last TRB in that TD before moving the dequeue pointer to the next TD. This will resolve some of the uvc and dvb issues with the "ERROR Transfer event TRB DMA ptr not part of current TD" error message Cc: <stable@vger.kernel.org> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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- 08 4月, 2015 1 次提交
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由 Felipe Balbi 提交于
Make sure we're using the new macro, so our resume signaling will always pass certification. Cc: <stable@vger.kernel.org> # v3.10+ Acked-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NFelipe Balbi <balbi@ti.com>
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- 18 3月, 2015 1 次提交
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由 Lin Wang 提交于
Some toggling operation in xHCI driver still use conditional toggling: ring->cycle_state = (ring->cycle_state ? 0 : 1); Use XOR to invert the cycle state instead of a conditional toggle to unify cycle state toggling operation in xHCI driver. Signed-off-by: NLin Wang <lin.x.wang@intel.com> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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- 11 3月, 2015 1 次提交
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由 Mathias Nyman 提交于
This reverts commit 27082e26 ("xhci: Clear the host side toggle manually") Turns out this fix to enable soft resetting endpoints wasn't mature enough. It caused regression with some usb DVB-T devices and needs some more tuning to get the endpiont ring pointers set correctly. The original commit was tagged for stable 3.18, and should be reverted from there as well. Cc: stable <stable@vger.kernel.org> # v3.18 Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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- 07 3月, 2015 1 次提交
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由 Aleksander Morgado 提交于
When a control transfer has a short data stage, the xHCI controller generates two transfer events: a COMP_SHORT_TX event that specifies the untransferred amount, and a COMP_SUCCESS event. But when the data stage is not short, only the COMP_SUCCESS event occurs. Therefore, xhci-hcd must set urb->actual_length to urb->transfer_buffer_length while processing the COMP_SUCCESS event, unless urb->actual_length was set already by a previous COMP_SHORT_TX event. The driver checks this by seeing whether urb->actual_length == 0, but this alone is the wrong test, as it is entirely possible for a short transfer to have an urb->actual_length = 0. This patch changes the xhci driver to rely on a new td->urb_length_set flag, which is set to true when a COMP_SHORT_TX event is received and the URB length updated at that stage. This fixes a bug which affected the HSO plugin, which relies on URBs with urb->actual_length == 0 to halt re-submitting the RX URB in the control endpoint. Cc: <stable@vger.kernel.org> Signed-off-by: NAleksander Morgado <aleksander@aleksander.es> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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- 25 2月, 2015 1 次提交
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由 Mathias Nyman 提交于
Main benefit of this is to get xhci connected USB scanners to work. Some devices use a clear endpoint halt request as a 'soft reset' even if the endpoint is not halted. This will clear the toggle and sequence on the device side. xHCI however refuses to reset a non-halted endpoint, so instead we need to issue a configure endpoint command on xHCI to clear its host side toggle and sequence, and get it in sync with the device side. Tested-by: NMike Mammarella <mikem@crystalorb.net> Cc: <stable@vger.kernel.org> # v3.18 Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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- 10 1月, 2015 3 次提交
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由 Mathias Nyman 提交于
Helps debugging to know the unhandled event type. Also make the debug message grepable Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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由 Lin Wang 提交于
Some parameters are not used by functions in xhci-mem.c, just remove it. Changes compared to v1: - Rebase to the latest usb-next branch Signed-off-by: NLin Wang <lin.x.wang@intel.com> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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由 Lin Wang 提交于
Parameter 'xhci' is no longer be used in function xhci_handshake(), just remove it. Signed-off-by: NLin Wang <lin.x.wang@intel.com> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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- 03 12月, 2014 2 次提交
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由 Mathias Nyman 提交于
Endpoints halted on errors, and endpoints stopped manually both used the same ep->stopped_td to store the halted or stopped td. this causes confusion and possible races. There is no longer a need to use the ep->stopped_td variable to store the halted TD. A halted endpoint is handled immediately and we can pass it to the handling function directly. Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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由 Mathias Nyman 提交于
Remove unnecessary else after return, dropping extra indentation depth. No functional changes. Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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- 22 11月, 2014 2 次提交
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由 Mathias Nyman 提交于
If a device is halted and reuturns a STALL, then the halted endpoint needs to be cleared both on the host and device side. The host side halt is cleared by issueing a xhci reset endpoint command. The device side is cleared with a ClearFeature(ENDPOINT_HALT) request, which should be issued by the device driver if a URB reruen -EPIPE. Previously we cleared the host side halt after the device side was cleared. To make sure the host side halt is cleared in time we want to issue the reset endpoint command immedialtely when a STALL status is encountered. Otherwise we end up not following the specs and not returning -EPIPE several times in a row when trying to transfer data to a halted endpoint. Fixes: bcef3fd5 (USB: xhci: Handle errors that cause endpoint halts.) Cc: <stable@vger.kernel.org> # v2.6.33+ Tested-by: NFelipe Balbi <balbi@ti.com> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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由 Mathias Nyman 提交于
A halted endpoint ring must first be reset, then move the ring dequeue pointer past the problematic TRB. If we start the ring too early after reset, but before moving the dequeue pointer we will end up executing the same problematic TRB again. As we always issue a set transfer dequeue command after a reset endpoint command we can skip starting endpoint rings at reset endpoint command completion. Without this fix we end up trying to handle the same faulty TD for contol endpoints. causing timeout, and failing testusb ctrl_out write tests. Fixes: e9df17eb (USB: xhci: Correct assumptions about number of rings per endpoint.) Cc: <stable@vger.kernel.org> #v2.6.35 Tested-by: NFelipe Balbi <balbi@ti.com> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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- 24 9月, 2014 5 次提交
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由 Hans de Goede 提交于
Lately (with the use of uas / bulk-streams) we have been seeing several cases where this error triggers (which should never happen). Add some extra logging to make debugging these errors easier. Signed-off-by: NHans de Goede <hdegoede@redhat.com> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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由 Hans de Goede 提交于
Even though a Set TR deq ptr command operates on a ring, and an endpoint can have multiple rings, we can have only one Set TR deq ptr command pending. When an endpoint with streams halts or is stopped to unlink urbs, there will only be at most one ring active / one td being executed (the td stopped_td points to). So when we reset the endpoint (for a halt), or the stop command completes, we will queue one Set TR deq ptr command at most, cancelled urbs on other stream rings then the one being executed will have there trbs turned to nops, and once the hcd gets around to execute that stream ring they will be simply skipped. So the SET_DEQ_PENDING flag in the endpoint is sufficient protection against starting the endpoing before all stream rings are cleaned up. Signed-off-by: NHans de Goede <hdegoede@redhat.com> Acked-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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由 Hans de Goede 提交于
Even if the stream for which the command was intended has been freed in the mean time. This ensures that things start rolling again after an unlink / halt. Signed-off-by: NHans de Goede <hdegoede@redhat.com> Acked-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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由 Hans de Goede 提交于
xhci_queue_new_dequeue_state is the only caller of queue_set_tr_deq and queue_set_tr_deq checks for SET_DEQ_PENDING, where as xhci_queue_new_dequeue_state sets it which is inconsistent. Simply fold the 2 into one is a nice cleanup and fixes the inconsistency. Signed-off-by: NHans de Goede <hdegoede@redhat.com> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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由 Hans de Goede 提交于
There are multiple reasons for this: 1) This fixes a missing check for xhci_alloc_command failing in xhci_handle_cmd_stop_ep() 2) This adds a warning when we cannot set the new dequeue state because of xhci_alloc_command failing 3) It puts the allocation of the command after the sanity checks in queue_set_tr_deq(), avoiding leaking the command if those fail 4) Since queue_set_tr_deq now owns the command it can free it if queue_command fails 5) It reduces code duplication Signed-off-by: NHans de Goede <hdegoede@redhat.com> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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- 20 8月, 2014 2 次提交
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由 Mathias Nyman 提交于
When we manually need to move the TR dequeue pointer we need to set the correct cycle bit as well. Previously we used the trb pointer from the last event received as a base, but this was changed in commit 1f81b6d2 ("usb: xhci: Prefer endpoint context dequeue pointer") to use the dequeue pointer from the endpoint context instead It turns out some Asmedia controllers advance the dequeue pointer stored in the endpoint context past the event triggering TRB, and this messed up the way the cycle bit was calculated. Instead of adding a quirk or complicating the already hard to follow cycle bit code, the whole cycle bit calculation is now simplified and adapted to handle event and endpoint context dequeue pointer differences. Fixes: 1f81b6d2 ("usb: xhci: Prefer endpoint context dequeue pointer") Reported-by: NMaciej Puzio <mx34567@gmail.com> Reported-by: NEvan Langlois <uudruid74@gmail.com> Reviewed-by: NJulius Werner <jwerner@chromium.org> Tested-by: NMaciej Puzio <mx34567@gmail.com> Tested-by: NEvan Langlois <uudruid74@gmail.com> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Cc: stable@vger.kernel.org Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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由 Hans de Goede 提交于
When using a Renesas uPD720231 chipset usb-3 uas to sata bridge with a 120G Crucial M500 ssd, model string: Crucial_ CT120M500SSD1, together with a the integrated Intel xhci controller on a Haswell laptop: 00:14.0 USB controller [0c03]: Intel Corporation 8 Series USB xHCI HC [8086:9c31] (rev 04) The following error gets logged to dmesg: xhci error: Transfer event TRB DMA ptr not part of current TD Treating COMP_STOP the same as COMP_STOP_INVAL when no event_seg gets found fixes this. Signed-off-by: NHans de Goede <hdegoede@redhat.com> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Cc: stable@vger.kernel.org Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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- 02 8月, 2014 1 次提交
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由 Hans de Goede 提交于
Signed-off-by: NHans de Goede <hdegoede@redhat.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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- 25 6月, 2014 2 次提交
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由 Mathias Nyman 提交于
The transfer burst count (TBC) field in xhci 1.0 hosts should be set to the number of bursts needed to transfer all packets in a isoc TD. Supported values are 0-2 (1 to 3 bursts per service interval). Formula for TBC calculation is given in xhci spec section 4.11.2.3: TBC = roundup( Transfer Descriptor Packet Count / Max Burst Size +1 ) - 1 This patch should be applied to stable kernels since 3.0 that contain the commit 5cd43e33 "xhci 1.0: Set transfer burst count field." Cc: stable@vger.kernel.org # 3.0 Suggested-by: NShiChun Ma <masc2008@qq.com> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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由 Mathias Nyman 提交于
Command completion events normally include command completion status, SLOT_ID, and a pointer to the original command. Reset device command completion SLOT_ID may be zero according to xhci specs 4.6.11. VIA controllers set the SLOT_ID to zero, triggering a WARN_ON in the command completion handler. Use the SLOT ID found from the original command instead. This patch should be applied to stable kernels since 3.13 that contain the commit 20e7acb1 "xhci: use completion event's slot id rather than dig it out of command" Cc: stable@vger.kernel.org # 3.13 Reported-by: NSaran Neti <sarannmr@gmail.com> Tested-by: NSaran Neti <sarannmr@gmail.com> Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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- 20 5月, 2014 4 次提交
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由 Mathias Nyman 提交于
Use one timer to control command timeout. start/kick the timer every time a command is completed and a new command is waiting, or a new command is added to a empty list. If the timer runs out, then tag the current command as "aborted", and start the xhci command abortion process. Previously each function that submitted a command had its own timer. If that command timed out, a new command structure for the command was created and it was put on a cancel_cmd_list list, then a pci write to abort the command ring was issued. when the ring was aborted, it checked if the current command was the one to be canceled, later when the ring was stopped the driver got ownership of the TRBs in the command ring, compared then to the TRBs in the cancel_cmd_list, and turned them into No-ops. Now, instead, at timeout we tag the status of the command in the command queue to be aborted, and start the ring abortion. Ring abortion stops the command ring and gives control of the commands to us. All the aborted commands are now turned into No-ops. If the ring is already stopped when the command times outs its not possible to start the ring abortion, in this case the command is turnd to No-op right away. All these changes allows us to remove the entire cancel_cmd_list code. The functions waiting for a command to finish no longer have their own timeouts. They will wait either until the command completes normally, or until the whole command abortion is done. Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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由 Mathias Nyman 提交于
Remove the per-device command list and handle_cmd_in_cmd_wait_list() and use the completion and status variables found in the command structure in the global command list. Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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由 Mathias Nyman 提交于
Create a list to store command structures, add a structure to it every time a command is submitted, and remove it from the list once we get a command completion event matching the command. Callers that wait for completion will free their command structures themselves. The other command structures are freed in the command completion event handler. Also add a check that prevents queuing commands if host is dying Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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由 Mathias Nyman 提交于
To create a global command queue we require that each command put on the command ring is submitted with a command structure. Functions that queue commands and wait for completion need to allocate a command before submitting it, and free it once completed. The following command queuing functions need to be modified. xhci_configure_endpoint() xhci_address_device() xhci_queue_slot_control() xhci_queue_stop_endpoint() xhci_queue_new_dequeue_state() xhci_queue_reset_ep() xhci_configure_endpoint() xhci_configure_endpoint() could already be called with a command structure, and only xhci_check_maxpacket and xhci_check_bandwidth did not do so. These are changed and a command structure is now required. This change also simplifies the configure endpoint command completion handling and the "goto bandwidth_change" handling code can be removed. In some cases the command queuing function is called in interrupt context. These commands needs to be allocated atomically, and they can't wait for completion. These commands will in this patch be freed directly after queuing, but freeing will be moved to the command completion event handler in a later patch once we get the global command queue up.(Just so that we won't leak memory in the middle of the patch set) Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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- 26 4月, 2014 1 次提交
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由 Julius Werner 提交于
We have observed a rare cycle state desync bug after Set TR Dequeue Pointer commands on Intel LynxPoint xHCs (resulting in an endpoint that doesn't fetch new TRBs and thus an unresponsive USB device). It always triggers when a previous Set TR Dequeue Pointer command has set the pointer to the final Link TRB of a segment, and then another URB gets enqueued and cancelled again before it can be completed. Further investigation showed that the xHC had returned the Link TRB in the TRB Pointer field of the Transfer Event (CC == Stopped -- Length Invalid), but when xhci_find_new_dequeue_state() later accesses the Endpoint Context's TR Dequeue Pointer field it is set to the first TRB of the next segment. The driver expects those two values to be the same in this situation, and uses the cycle state of the latter together with the address of the former. This should be fine according to the XHCI specification, since the endpoint ring should be stopped when returning the Transfer Event and thus should not advance over the Link TRB before it gets restarted. However, real-world XHCI implementations apparently don't really care that much about these details, so the driver should follow a more defensive approach to try to work around HC spec violations. This patch removes the stopped_trb variable that had been used to store the TRB Pointer from the last Transfer Event of a stopped TRB. Instead, xhci_find_new_dequeue_state() now relies only on the Endpoint Context, requiring a small amount of additional processing to find the virtual address corresponding to the TR Dequeue Pointer. Some other parts of the function were slightly rearranged to better fit into this model. This patch should be backported to kernels as old as 2.6.31 that contain the commit ae636747 "USB: xhci: URB cancellation support." Signed-off-by: NJulius Werner <jwerner@chromium.org> Cc: stable@vger.kernel.org Signed-off-by: NMathias Nyman <mathias.nyman@linux.intel.com> Signed-off-by: NGreg Kroah-Hartman <gregkh@linuxfoundation.org>
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- 05 3月, 2014 6 次提交
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由 Sarah Sharp 提交于
If the host controller stops responding to commands, we need to kill all the URBs that were queued to all endpoints. The current code would only kill URBs that had been queued to the endpoint rings. ep->ring is set to NULL if streams has been enabled for the endpoint, which means URBs submitted with a non-zero stream_id would never get killed. Fix this. Signed-off-by: NSarah Sharp <sarah.a.sharp@linux.intel.com>
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由 Sarah Sharp 提交于
In preparation for fixing this function for streams endpoints, refactor code in the command watchdog timeout function into two new functions. One kills all URBs on a ring (either stream or endpoint), the other kills all URBs associated with an endpoint. Fix a split string while we're at it. Signed-off-by: NSarah Sharp <sarah.a.sharp@linux.intel.com>
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由 Hans de Goede 提交于
This fixes TR dequeue validation failing on Intel XHCI controllers with the following warning: Mismatch between completed Set TR Deq Ptr command & xHCI internal state. Interestingly enough reading the deq ptr from the ep ctx after a TR Deq Ptr command does work on a Nec XHCI controller, it seems the Nec writes the ptr to both the ep and stream contexts when streams are used. Signed-off-by: NHans de Goede <hdegoede@redhat.com> Signed-off-by: NSarah Sharp <sarah.a.sharp@linux.intel.com>
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由 Hans de Goede 提交于
Nec XHCI controllers don't seem to care, but without this Intel XHCI controllers reject Set TR dequeue commands with a COMP_TRB_ERR, leading to the following warning: WARN Set TR Deq Ptr cmd invalid because of stream ID configuration And very shortly after this the system completely freezes. Signed-off-by: NHans de Goede <hdegoede@redhat.com> Signed-off-by: NSarah Sharp <sarah.a.sharp@linux.intel.com>
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由 Hans de Goede 提交于
Signed-off-by: NHans de Goede <hdegoede@redhat.com> Signed-off-by: NSarah Sharp <sarah.a.sharp@linux.intel.com>
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由 Oliver Neukum 提交于
This changes debug messages and warnings in xhci-ring.c to be on a single line so grep can find them. grep must have precedence over the 80 column limit. [Sarah fixed two checkpatch.pl issues with split lines introduced by this commit.] Signed-off-by: NOliver Neukum <oneukum@suse.de> Signed-off-by: NSarah Sharp <sarah.a.sharp@linux.intel.com>
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- 08 2月, 2014 1 次提交
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由 Sarah Sharp 提交于
This reverts commit 35773dac. It's a hack that caused regressions in the usb-storage and userspace USB drivers that use usbfs and libusb. Commit 70cabb7d992f "xhci 1.0: Limit arbitrarily-aligned scatter gather." should fix the issues seen with the ax88179_178a driver on xHCI 1.0 hosts, without causing regressions. Signed-off-by: NSarah Sharp <sarah.a.sharp@linux.intel.com> Cc: stable@vger.kernel.org # 3.12
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