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由 Ilan Peer 提交于
The cmd_in_flight tracking was introduced to workaround faulty power management hardware, by having the driver keep the NIC awake as long as there are commands in flight. However, some of the code handling this workaround was unconditionally executed, which resulted with an inconsistent state where the driver assumed that the NIC was awake although it wasn't. Fix this by renaming 'cmd_in_flight' to 'cmd_hold_nic_awake' and handling the NIC requested awake state only for hardwares for which the workaround is needed. Signed-off-by: NIlan Peer <ilan.peer@intel.com> Signed-off-by: NEmmanuel Grumbach <emmanuel.grumbach@intel.com>
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