提交 94bef000 编写于 作者: M Matt Ranostay 提交者: Jonathan Cameron

iio: hudmidity: hdc100x: fix incorrect shifting and scaling

Shifting sensor data to the right 2 bits was incorrect and caused the
scaling values + offsets to be invalid.
Reported-by: NAlison Schofield <amsfield22@gmail.com>
Signed-off-by: NMatt Ranostay <mranostay@gmail.com>
Tested-by: NAlison Schofield <amsfield22@gmail.com>
Cc: <Stable@vger.kernel.org>
Signed-off-by: NJonathan Cameron <jic23@kernel.org>
上级 590b92a3
......@@ -164,14 +164,14 @@ static int hdc100x_get_measurement(struct hdc100x_data *data,
dev_err(&client->dev, "cannot read high byte measurement");
return ret;
}
val = ret << 6;
val = ret << 8;
ret = i2c_smbus_read_byte(client);
if (ret < 0) {
dev_err(&client->dev, "cannot read low byte measurement");
return ret;
}
val |= ret >> 2;
val |= ret;
return val;
}
......@@ -212,17 +212,17 @@ static int hdc100x_read_raw(struct iio_dev *indio_dev,
case IIO_CHAN_INFO_SCALE:
if (chan->type == IIO_TEMP) {
*val = 165000;
*val2 = 65536 >> 2;
*val2 = 65536;
return IIO_VAL_FRACTIONAL;
} else {
*val = 0;
*val2 = 10000;
return IIO_VAL_INT_PLUS_MICRO;
*val = 100;
*val2 = 65536;
return IIO_VAL_FRACTIONAL;
}
break;
case IIO_CHAN_INFO_OFFSET:
*val = -3971;
*val2 = 879096;
*val = -15887;
*val2 = 515151;
return IIO_VAL_INT_PLUS_MICRO;
default:
return -EINVAL;
......
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