Revert "ARM: OMAP3530evm: set pendown_state and debounce time for ads7846"
1) The above commit introduced a common ->get_pendown_state() function into the generic code, but that function was board-specific for the OMAP3EVM and thus broke most other boards using this code. 2) The above commit was mis-merged introducing another bug which prevents the ads7846 driver probe function to succeed. The omap_ads7846_init() function frees the pendown GPIO in case there is no ->get_pendown_state() function set by the caller (board specific code), so it can be requested later by the ads7846 driver. The above commit add a common ->get_pendown_state() function without removing the gpio_free() call and thus once the ads7846 driver tries to use the pendown GPIO, it crashes as the pendown GPIO has not been requested. 3) The above commit introduces NO new functionality as get_pendown_state() function is already implemented in a suitable way by the ads7846 driver and the debounce time handling has already been fixed by commit 97ee9f01 (ARM: OMAP: fix the ads7846 init code). This reverts commit 16aced80. Conflicts: arch/arm/mach-omap2/common-board-devices.c Solved by taking the working version prior to the above commit. Cc: Zumeng Chen <zumeng.chen@windriver.com> Cc: Arnd Bergmann <arnd@arndb.de> Signed-off-by: NIgor Grinberg <grinberg@compulab.co.il> Reviewed-by: NKevin Hilman <khilman@ti.com> Tested-by: NKevin Hilman <khilman@ti.com> Signed-off-by: NKevin Hilman <khilman@ti.com>
Showing
想要评论请 注册 或 登录