diff --git a/hw/gusemu.h b/hw/gusemu.h index 34872aa101a8772f620fc23781dca1f59ef9937d..331bb6fec0036f979d4adf61df59258f5c2b6ec8 100644 --- a/hw/gusemu.h +++ b/hw/gusemu.h @@ -27,7 +27,7 @@ /* data types (need to be adjusted if neither a VC6 nor a C99 compatible compiler is used) */ -#if defined _WIN32 && defined _MSC_VER /* doesnt support other win32 compilers yet, do it yourself... */ +#if defined _WIN32 && defined _MSC_VER /* doesn't support other win32 compilers yet, do it yourself... */ typedef unsigned char GUSbyte; typedef unsigned short GUSword; typedef unsigned int GUSdword; diff --git a/hw/rtl8139.c b/hw/rtl8139.c index aa8ed0a919d8ef7ab3a0ce6e647fff0366d6413e..8aace9a4ec4cb057b8c698550f0f22bb3575a406 100644 --- a/hw/rtl8139.c +++ b/hw/rtl8139.c @@ -2662,7 +2662,7 @@ static void rtl8139_IntrStatus_write(RTL8139State *s, uint32_t val) * Computing if we miss an interrupt here is not that correct but * considered that we should have had already an interrupt * and probably emulated is slower is better to assume this resetting was - * done before testing on previous rtl8139_update_irq lead to IRQ loosing + * done before testing on previous rtl8139_update_irq lead to IRQ losing */ rtl8139_set_next_tctr_time(s, qemu_get_clock_ns(vm_clock)); rtl8139_update_irq(s); diff --git a/hw/ssd0303.c b/hw/ssd0303.c index 401fdf592a54259e65fa4bb0e7a271ebea3b6941..bcad7bf9229c9c4889bbf9b0e6d1792f44da6fc6 100644 --- a/hw/ssd0303.c +++ b/hw/ssd0303.c @@ -123,7 +123,7 @@ static int ssd0303_send(i2c_slave *i2c, uint8_t data) case 0xa7: /* Inverse on. */ s->inverse = 1; break; - case 0xa8: /* Set multipled ratio (Ignored). */ + case 0xa8: /* Set multiplied ratio (Ignored). */ s->cmd_state = SSD0303_CMD_SKIP1; break; case 0xad: /* DC-DC power control. */